请输入您要查询的百科知识:

 

词条 FG-15
释义

  1. See also

  2. References

{{Infobox rocket engine
|name =FG-15B
|image =
|image_size =
|caption =
|country_of_origin=China
|date =
|first_date =1986-02-02
|last_date =
|designer =China Hexi Chemical and Machinery Corporation
|manufacturer =
|purpose =Apogee kick motor
|associated =Long March 3
|predecessor =FG-02
|successor =FG-36
|status =Out of Production
|type =solid
|oxidiser =
|fuel =HTPB
|grain =
|core =
|casing =Fiberglass
|nozzle =
|description =
|combustion_chamber=1
|nozzle_ratio =
|thrust =
|thrust_at_altitude=
|thrust(Vac) ={{convert|40.9|kN|lbf|abbr=on}}
|thrust(SL) =
|thrust_to_weight=
|chamber_pressure=
|specific_impulse=
|specific_impulse_vacuum={{convert|289|isp|abbr=on}}
|specific_impulse_sea_level=
|total_impulse ={{convert|1.432|MN|abbr=on}}
|burn_time =35s
|gimbal =
|capacity ={{convert|505|kg|lb|abbr=on}}
|dimensions =
|length ={{convert|1489|mm|in|abbr=on}}
|diameter ={{convert|896|mm|in|abbr=on}}
|dry_weight ={{convert|75|kg|lb|abbr=on}}
|used_in =Dong Fang Hong 2
|references =[1][2]
|notes =
}}

The FG-15 (AKA DFH-2 AKM and SpaB-170) was a Chinese spin stabilized apogee kick motor burning HTPB. It was developed by China Hexi Chemical and Machinery Corporation (also known as the 6th Academy of CASIC) for use in the Dong Fang Hong 2 satellite bus for insertion into GSO orbit.[5]

It has a total nominal mass of {{convert|580|kg|lb|abbr=on}}, of which {{convert|505|kg|lb|abbr=on}} is propellant load and its burn out mass is {{convert|75|kg|lb|abbr=on}}. It has an average thrust of {{convert|40.9|kN|lbf|abbr=on}} with a specific impulse of 289 seconds burning for 35 seconds, with a total impulse of {{convert|1.432|MN|abbr=on}}. This motor introduced a series of innovations for the Chinese solid motor industry: first use of glass fibre wound cases, carbon/carbon nozzle throat insert material, contoured divergent nozzle, and non-destructive test of the motor grain.

The initial version had the manufacturing code FG-15 was associated to the DFH-2 bus and flew twice. The FG-15B was used by the DFH-2A bus and flew five times.

DateCarrier RocketMotorLaunch siteMissionResult
1984-01-29 Long March 3 FG-15 Xichang Satellite Launch Center STTW-T1 Failure to ignite
1984-04-09 Long March 3 FG-15 Xichang Satellite Launch Center STTW-T2 Success
1986-02-02 Long March 3 FG-15B Xichang Satellite Launch Center DFH-2A-T1 Success
1988-03-09 Long March 3 FG-15B Xichang Satellite Launch Center ChinaSat-1 (DFH-2A-T2) Success
1998-12-24 Long March 3 FG-15B Xichang Satellite Launch Center DFH-2A-T3 Success
1990-02-05 Long March 3 FG-15B Xichang Satellite Launch Center DFH-2A-T4 Success
1991-12-28 Long March 3 FG-15B Xichang Satellite Launch Center ChinaSat-4 (DFH-2A-T5) Failure to ignite

See also

  • China Hexi Chemical and Machinery Corporation
  • Dong Fang Hong 2
  • Long March 3

References

1. ^{{cite web |url=http://www.astronautix.com/engines/dfh2akm.htm |title=DFH-2 AKM |publisher=Encyclopedia Astronautica |accessdate=2015-07-25 |deadurl=yes |archiveurl=https://web.archive.org/web/20140209184540/http://www.astronautix.com/engines/dfh2akm.htm |archivedate=2014-02-09 |df= }}
2. ^{{cite book |url=https://books.google.com.ar/books?id=hZBAAAAAQBAJ&pg=PA97&lpg=PA97&dq=GF-36 |title=China's Space Program — The Great Leap Forward |last=Harvey |first=Brian |chapter=Rocket Engines |page=97 |publisher=Springer Science & Business Media |date=2013 |isbn=978-1461450436 |access-date=2015-07-25}}
3. ^{{cite web |url=http://planet4589.org/space/book/lv/engines/motorlist/shanxiakm.html |title=5.6.38: Shanxi AKM |last=McDowell |first=Jonathan |publisher=Jonathan Space Report |accessdate=2015-07-25}}
[1][2][3]
}}{{Orbital spacecraft rocket engines}}{{DEFAULTSORT:FG-15}}{{rocket-stub}}

2 : Rocket engines of China|Solid-fuel rockets

随便看

 

开放百科全书收录14589846条英语、德语、日语等多语种百科知识,基本涵盖了大多数领域的百科知识,是一部内容自由、开放的电子版国际百科全书。

 

Copyright © 2023 OENC.NET All Rights Reserved
京ICP备2021023879号 更新时间:2024/9/24 0:30:35